Washing machine repair saga

--- In April 2025 it failed again see update at bottom of this page. --- Jan. 2024: This is a rewrite of the saga of fixing our washing machine now that it is finally fixed. The integration of images and text is done in a rather crude way with preformatted text and line spacing... I'd be interested in hearing if this does / not work with your browser. It looks ok with Firefox on my desktop computer. I have not looked at it with a cell phone... Note to those browsing with a smart phone Fred fholson [at] cohousing.org 612-588-9532 In mid November 2023 we noticed that the agitator of our 1985 vintage Whirlpool washing machine (Model LA5580XM ) was barely moving. It may have been this way for some time - who watches the washing machine while it's running? At first I expected it to be an easy fix. There are numerous Youtube videos on fixing the problem by replacing the "Agitator Directional Cogs" in the top of the agitator. But the procedure did not apply to our 1985 machine. For starters our agitator is assembled differently. The basic problem was that the agitator (the plastic part) turned fairly freely in either direction relative to the steel drive shaft that should drive it. Older machines are reputedly more durable and trouble free. And it seemed like a fairly simple problem -- to get the steel shaft to turn the plastic agitator. I made numerous attempts here in North Minneapolis -- trying various approches, consulting others, taking the problem with pictures (but not the machine...) to a fixit clinic, getting a repair manual that did not address our specific problem. All failed to solve the problem. I became obsesssed with fixing it. We did look at new machines and found used Speed Queen machines that have a great reputation. We washed clothes at friend's. I finally came up with a unique approach and got it working in early March 2024. It only took about 4 months to fix it... What follows is a chronlogical description modtly keyed to images I took along the way of various attempts to fix it, ending with a description the fix that worked. Image:agitator before repair Our agitator appeared to be held on by a nut on a 3/8 inch threaded rod (3/8") presumably coming from the top of the drive shaft. But since the drive shaft turned relative to the plastic agitator there was no way to hold the shaft from turning to unscrew the nut. I looked under the tub for a way to hold the shaft but found none. Image:3/8 inch nut with cut I cut half way thru a another 3/8" nut and threaded it onto the threaded rod at the top of the agitator, leaving a gap between the "cut nut" and the nut holding the agitator. Using a vice grip to clamp the "cut nut" very tightly around the threads (and protect them) to hold the shaft and a box end wrench on the other nut I tried to loosen the latter. This failed to allow unscrewing the "nut". After closer examination of the agitator "nut", I concluded that this "nut" was an integral part of the threaded rod. If true, this implied that it was a stud; that is it had threads on both ends, This stud is special having a head in the middle. I later learned it has different threads on each end. One end of the stud is screwed into the top of the drive shaft. But getting it loose still required holding the drive shaft still. I tried bolting a box end wrench on the head of the stud and hitting it with a big hammer (I do not have an impact wrench.) Still no luck. Image:agitator shaft illustration with stud and with grooves About this time I pursued getting a 1985 vintage repair manual by interlibrary loan. Thanks to Natalie Hart of Sumner Library. It took several weeks and two attempts to get one from Indiana. Tho it did not correspond to our machine's agitator assembly exactly, it is very close. This image from the manual showed the stud screwed into the top of the drive shaft. Note that unlike our machine, the stud is under the plastic agitator which is held on by a plastic cap above the agitator that screws onto the stud. On ours, the stud head is on top of the plastic agitator and holds it on. This image from the manual showed that the plastic agitator engaged the drive shaft with grooves. Apparently the grooves in our agitator or shaft were stripped. But since I could not get the agitator off I could not be sure. Image:agitator with small bolts in drilled holes I had started pondering drilling thru the plastic to try and grip the shaft somehow. I drilled 3 (5/32") holes spaced around the agitator thru the plastic agitator but my drill bit did not seem sharp enough to drill into the shaft much. I cut off nails to go in the holes. Note this image is actually from later but looks very similar to the nails version; it has hex head bolts instead of nails. The stud is not shown in this later image. Image:agitator with bolts and screw clamp I put a stainless steel screw clamp around the nails to hold them in. Again this image is from later but similar to this stage of the saga. This improved the connection between the shaft and the agitator but when I tried using the machine (with water and clothes) it agitated about 30 degrees back and forth while the stud rotated about 180 degrees. I thought maybe if I could hold the nails tighter to the shaft than the screw clamp allowed it would work better. I considered a short section of steel pipe around nails and wedges driven between the nails and pipe to get more grip between shaft and agitator. I went to my local hardware store to get a better drill bit. I discussed possible fixes in depth with John Guion at North End Hardware and got some ideas about possible approaches. Suitable pipe would be availble there but not suitable wedges. I did not know how long the pipe piece should be on that trip. I got neither at that time. John suggested drilling and tapping holes in the pipe for set screws. This is a great idea but getting the drilled holes to line up with the existing holes in the plastic agitator seemed like a big challenge and I did not want to drill more holes in the plastic. John also suggested bolting a very large washer onto the stud to hold the pipe, wedges or screw clamp in place. Image:2 bolts -- before and after grinding I drilled holes in the shaft and made better set screws to go in them. Using the very hard cobalt 5/32" drill bit, I easily made holes in the shaft about 3/16". Unfortunately the tub prevented the drill from being at right angles. It was maybe 75-80 degrees. (see "offset" below") I carefully measured the depth of the hole and used oil and drilled slowly as John suggested. I ground down 1/4" fine threaded, hardened bolts to serve as set screws. Image shows 2 bolts -- before and after grinding. Image:agitator with bolts - stud removed I enlarged the holes in the plastic to 1/4 inch. The set screws threaded into the plastic. When screwed in completely the end of the set screw goes into the hole in the shaft. This greatly increases the connection between the agitator and the shaft. In this image one set screw is not screwed in far to show itself. Image:agitator with bolts and screw clamp But since the plastic is not strong enough to hold the set screws very well, I used the screw clamp to hold them into the holes. The set screws now went into the shaft. Image:the stud removed Once the agitator gripped the shaft I got the stud out! Image:agitator shaft With the stud out I removed the agitator. The drive shaft surface where it engaged the agitator is very corroded and there is almost no sign of grooves. Image:agitator shaft This image of the shaft is a bit blurry but does show one of the drilled holes into it. These holes and the set screws (ground down bolts) that go in them are what really make the connection between the shaft and the plastic agitator. Image:inside of the plastic agitator This image is the inside of the plastic agitator from the bottom. The grooves that should engage the shaft are so far in it is hard to observe their condition. Getting the agitator off did allow me to refine holes in the shaft that the set screws engage. I measured the depth of the holes in the shaft better. Note that much more depth would encounter the thread where the stud screws into. Image:agitator with clamp over bolts (not visible) and large washer So here is how the assembled repair looks. Note the large washers bolted to the stud to hold the clamp in place. Image:Right angle drill Note that where 3 set screws go thru the plastic are exposed to all the forces. If they wear the plastic this fix could fail. An alternative would be to put more holes and set screws below the existing ones. This would require an offset drill like this to drill holes at a right angle. North End Hardware rents them.

April 2025 update.

After about a year my fix failed and the agitator is not turning much. That is the plastic agitator does not turn with the drive shaft - not much at least. I am again having trouble removing the "stud" that holds the agitator on. I am thinking of drilling a 1/4" hole all the way thru the shaft below where the stud screws in and putting a stainless steel bolt all the way thru. This will require renting an offset drill (above) Image:Close quarters drill A few days after writing the above... I did rent a drill at my local hardware store but the chuck was not a full 90 degrees from the handle. I bought a cobalt 1/4" bit. There was not space to start the bit at 90 degrees tho close. I drilled thru the plastic agitator at this angle and then got to 90 degrees from the the shaft. I was careful to be aligned properly to go thru the center the shaft as well a possible. It was not too difficult to drill the hole and it came out about the right place on the far side. I rented the drill for the 2 hour minimum but it only took about an hour including returning the drill by bicycle. So far this fix looks great. I have not gotten the "stud" out again but decided I do not really need to.

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